Ok, back at it tonight with Josh again coming by to lend his growing expertise.

Before Josh got here I pulled the 009 and rebuilt the "innards" of the original vacuum "shorty" distributor. Also I redid all the fuel lines since the stuff I got from the Porsche dealer in North Olmsted was already starting to fray.

Looks like it was high end 5mm stuff, but the black cloth braiding was coming off the rubber and kind of scaring me. I went back to the cloth VW stuff.
So the engine didn't run. The cap was bad and it's some kind of "one year or so only" cap. Eventually we did a little modification to run it with only the vacuum distributor.

Turns out it wasn't advancing just staying at 10 degrees BTDC when we tried to dial it in. Don't know what's up 'cause the suction test worked.

It really didn't matter since it was really the carb that was the problem. Josh kept saying carb and I kept saying distributor, but in the end he was right.

He figured the carb was the one thing that "changed" since the rebuild, so it had to be that. On the other hand, I'm older and wiser

and believe everything with a VW is broken until its proven to work, so I took the other approach.
Anyway, Josh came prepared. First he put the SVDA from aircooled.net he got for his '71 bus on my motor and we went for a ride. Better, but still problems. It's not the disitributor announces Josh.

So I say the carb won't help any and it's still the distributor!

So along with the SVDA Josh throws on his working 28 PCI. Even without vacuum this engine just purrrs. Great acceleration, no flat spot, power galore and a smooth ride. So now even I'm thinking CARB!

I dig into my stash and find two old 28 PCI's with a few old rebuild kits. Josh and I started laughing when we saw one was marked $1.40. They are selling now on WW for $24.99.
So we pick what we think is the better of the two carbs, it wasn't!

We do a driveway rebuild with California Quality

and we get more hesitation and heat. Off that one comes. On goes the other one. Better, but still issues. Crud was floating around like no tomorrow!

Oh and I forgot we bolted the second one up only to discover it had no upper gasket and no float bowl! Oh yea, that ran like a champ!
So we did the driveway rebuild, "part two", and this one seems to have some promise, but still showing problems. The jets need to be cleaned because I bet they're clogged. Josh knows they're clogged!

We drove it around the block, but were getting hungry and thristy so we had to head up to Panini's.
Before we finished up we did the Generator ploarization test. Seems we got it right and the generator spun, but the red light is still on.

We did a test at the battery. 6.2 volts accros the terminals when the engine was off. It did not go up with the engine running at higher RPM's, so it may be we have a bad generator. Unless someone thinks it's something else????
All in all we had a great time doing the forensics!
Tomorrow is another day!
