Well, it started out simple and innocent enough, a valve lash adjuster loosened up, the nut walked off, the screw backed out and the pushrod fell out. This caused constant backfiring into the intake manifold because it was an exhaust valve not opening. No sweat, put that back together, adjust the valves, good to go, right?
The fan belt's loose, better take care of that. Crap, the nut's all mucked up with the threads gone
and deposited them on the gen shaft.
No sweat, we have the technology. Chase the threads,
Find a nice German nut and washer thing in my junk,
And we're good to go. Easy, peasy, she'll be happy, right?
